TY - JOUR
T1 - Investigation on the impact of protrusion parameter on the efficiency of converting additional windage loss for ingress alleviation in rotor-stator system
AU - Liu, Dongdong
AU - Tao, Zhi
AU - Luo, Xiang
AU - Kang, Wenwu
AU - Wu, Hongwei
AU - Yu, Xiao
PY - 2016/6/28
Y1 - 2016/6/28
N2 - This paper presents a detailed investigation on the impact of protrusion parameter including both radial position and amount on the efficiency of cavity with protrusion converting additional windage loss for ingress alleviation in rotor–stator system. Experiment is conducted to explore the effect of protrusion parameter on ingress, and the corresponding additional windage loss is also calculated. During the experiment, rotor-mounted protrusions are circumferentially assembled at three different radial positions (0.9b, 0.8b, and 0.7b) each with four different amounts (32, 24, 16, and 8). Measurements of CO2 concentration and pressure inside turbine cavity are conducted. In the experiment, the annulus Reynolds number and rotating Reynolds number are set at 1.77 × 105 and 7.42 × 105, respectively, while the dimensionless sealing air flow rate ranges from 3047 to 8310. Experimental result shows that the cases of protrusion set at 0.8b achieve higher sealing efficiency than other cases as the cavity pressure is enhanced. The effect of protrusion amount on ingress could be obviously seen when CW is small or protrusion set in 0.7b. Furthermore, a parameter to evaluate which case obtains higher efficiency of converting additional windage loss for ingress alleviation, or alleviates ingress more efficiently for short, is applied for discussion. It is found that the case “C, N = 8” alleviates ingress most efficiently among all the cases. Therefore, proper setting of the protrusion could lead to high efficiency of converting additional windage loss for ingress alleviation in rotor–stator system.
AB - This paper presents a detailed investigation on the impact of protrusion parameter including both radial position and amount on the efficiency of cavity with protrusion converting additional windage loss for ingress alleviation in rotor–stator system. Experiment is conducted to explore the effect of protrusion parameter on ingress, and the corresponding additional windage loss is also calculated. During the experiment, rotor-mounted protrusions are circumferentially assembled at three different radial positions (0.9b, 0.8b, and 0.7b) each with four different amounts (32, 24, 16, and 8). Measurements of CO2 concentration and pressure inside turbine cavity are conducted. In the experiment, the annulus Reynolds number and rotating Reynolds number are set at 1.77 × 105 and 7.42 × 105, respectively, while the dimensionless sealing air flow rate ranges from 3047 to 8310. Experimental result shows that the cases of protrusion set at 0.8b achieve higher sealing efficiency than other cases as the cavity pressure is enhanced. The effect of protrusion amount on ingress could be obviously seen when CW is small or protrusion set in 0.7b. Furthermore, a parameter to evaluate which case obtains higher efficiency of converting additional windage loss for ingress alleviation, or alleviates ingress more efficiently for short, is applied for discussion. It is found that the case “C, N = 8” alleviates ingress most efficiently among all the cases. Therefore, proper setting of the protrusion could lead to high efficiency of converting additional windage loss for ingress alleviation in rotor–stator system.
KW - Ingestion
KW - protrusion
KW - experiment
KW - windage loss
UR - https://www.scopus.com/pages/publications/84976869260
U2 - 10.1115/1.4033617
DO - 10.1115/1.4033617
M3 - Article
SN - 0742-4795
SN - 1528-8919
VL - 138
SP - 112604
JO - Journal of Engineering for Gas Turbine and Power
JF - Journal of Engineering for Gas Turbine and Power
IS - 11
ER -